RESULTS:
White/Red on MAF to Ground = 13.05v - 13.09v (fluctuate)
**** This is your supply and this is good
Black on MAF to Ground DOES NOT EXIST... however, Black/Red on MAF to Ground = .06v (steady)
**** This is your ground and that is good as well
Green on MAF to ground DOES NOT EXIST ... however, Green/Black on MAF to Ground = .23v - .25v (fluctuate)
**** This is your output to your ECU. Voltage should read between 2 to 5 Volts while the car is running. Check at the ECU where doest it connect to ?
Blue on O2 sensor to Ground = 0.0v (steady)
**** This is not normal( Trying toi figure out why )
White on 02 sensor to Ground = -.06v to -.07v (fluctuate)
**** This is normal, I believe it is your sensor ground which connects to pin 91 on the ECU.
The Two Black on the O2 sensor to ground = 6.5v - 10.5v (fluctuate)
**** I am not sure what these are. 1 of them is the heater and the other seems to be connecting to the cooling fan relay.
Some things that i noticed:
Last night what corrected the idle: Pink/blue and Blue/yellow (signal from first and second o2..i think thats what the blue/yellow is) are joined by a black/white wire at the harness which splits and connects to each one. i cut the line (part of the V if you call it that) from the black/white wire going to the pink/blue at pin60, and idle corrected and the car worked good all last night and today. i reconnected the wire to be more accurate on this test you had me do (since im sure that wire wasnt supposed to be cut), and BAM bad idle again, and ive got fuel/carbon/sludge pilling up in my muffler from running so rich. i dont know what this means.
Almost stalling: i dont know what the Green/Black wire is on the MAF, but when i hook up the multimeter to it, the car goes from higher rpm at idle to almost completely dead, over and over and over until i stop testing.
Timm to answer your question: when i took out the clamp last night, it did absolutely nothing different. when i DISCONNECTED the wire leading tothe pink/blue at the harness (see above), then it drove like stock (good idle, lean immediately upon entering boost). then i put the clamp BACK in with the wire that heads to pink/blue at the harness STILL disconnected, and it boosted like a good ole boy all last night and today. it stopped working on my way home from work.