Overboost on stock setup... ongoing problem. (!!UPDATE NEW TURBO!!!)
UPDATE!!!!!!!!!!!! SO i took it into service because it was making that whine sound from the wg, they called mazda and the next day i had a new turbo and wg acuator, everything is perfect now. Boosts 6.5 stock, and with unichip 10-12.
Wierd thing is, it deffinitlly pulls harder @ 6psi than it used 2, ive had a few friends in teh car and they noticed it without me saying anything about a new turbo. I wonder if the "turkey" compressor surge... actually causes a decrease in performance after some miles... hrm... o well fmic and a addition bov here i come... anyway wanna loan me 1500$???
Hey guys, been about 8 months since ive posted here, dealing with life. Anyway im starting to get some time to deal with some problems ive been having with my msp from way back.
When i first got this car (my second msp) it was making 6 pounds with MAYBE a 1/2 pound overboost. Threw on the corksport 2.5" exhaust and would get a 1 to 1 &1/2 pound overboost, no biggie. A few weeks later i threw on the unichip. Everything worked fine, 6-7&1/2 pounds on stock boost, 10-13 pounds once i switched the unichip boost controller on. Worked fine for about i dono maybe 2 months. Then one day i started seeing 15-17 pounds!!! i swaped the boost guage and got the same results. If i was running stock boost map, it wouldnt overboost at all but as soon as i switched to the higher boost map it would spike to around 17 and steady around 15psi!!!!
I talked with unichip, repalced the boost solinoid(sp) with the same results. Eventually i got wrapped up in life and quit worrying about running more than stock boost.
So here Iam 20k miles later with the same problem, only now, even on stock boost sometimes i get a spike of 10psi and it sits around 8. I dont dare try and switch the boost controller on for fear of having a 20psi msp... for about 200 feet anyway.
So i guess what im asking for is if anyone who has been on the boards more has seen anyone with the same problem....or maybe somethin similar? heard anything like this?
All the information ive gotten has pointed to the wastegate actuator as the problem. The thing is you cant order just the actuator from mazda, you have to order the ENTIRE assembly for almost 3k!
Thanks guys and sorry if some of the words are ****** up, im trying to type on one of those dam ergonmic keyboards.
UPDATE!!!!!!!!!!!! SO i took it into service because it was making that whine sound from the wg, they called mazda and the next day i had a new turbo and wg acuator, everything is perfect now. Boosts 6.5 stock, and with unichip 10-12.
Wierd thing is, it deffinitlly pulls harder @ 6psi than it used 2, ive had a few friends in teh car and they noticed it without me saying anything about a new turbo. I wonder if the "turkey" compressor surge... actually causes a decrease in performance after some miles... hrm... o well fmic and a addition bov here i come... anyway wanna loan me 1500$???
Hey guys, been about 8 months since ive posted here, dealing with life. Anyway im starting to get some time to deal with some problems ive been having with my msp from way back.
When i first got this car (my second msp) it was making 6 pounds with MAYBE a 1/2 pound overboost. Threw on the corksport 2.5" exhaust and would get a 1 to 1 &1/2 pound overboost, no biggie. A few weeks later i threw on the unichip. Everything worked fine, 6-7&1/2 pounds on stock boost, 10-13 pounds once i switched the unichip boost controller on. Worked fine for about i dono maybe 2 months. Then one day i started seeing 15-17 pounds!!! i swaped the boost guage and got the same results. If i was running stock boost map, it wouldnt overboost at all but as soon as i switched to the higher boost map it would spike to around 17 and steady around 15psi!!!!
I talked with unichip, repalced the boost solinoid(sp) with the same results. Eventually i got wrapped up in life and quit worrying about running more than stock boost.
So here Iam 20k miles later with the same problem, only now, even on stock boost sometimes i get a spike of 10psi and it sits around 8. I dont dare try and switch the boost controller on for fear of having a 20psi msp... for about 200 feet anyway.
So i guess what im asking for is if anyone who has been on the boards more has seen anyone with the same problem....or maybe somethin similar? heard anything like this?
All the information ive gotten has pointed to the wastegate actuator as the problem. The thing is you cant order just the actuator from mazda, you have to order the ENTIRE assembly for almost 3k!
Thanks guys and sorry if some of the words are ****** up, im trying to type on one of those dam ergonmic keyboards.
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