Survived the VICS recall "event" (44k miles)since was idling into driveway when happened. Got into garage, fished out the single screw from cyl 3. Had only made 6-8 taps at low rpm before motor was shut off. No CEL. No closed gap on plug. 2 butterflies in bottom of intake that wallowed over remaining loose screws. Only 1 screw actually out, all others loose. Pulled apart, red loctited new screws in on VICS, removed VTCS, put on new int gasket on head, cleaned egr, did coolant buypass on TB, put it all back & running better than ever today. Close call, lucky not on freeway when it came off!