I've had Tony's header on for about 4-1/2 weeks now, and I have no complaints. There aren't any leaks (I used Coppercoat on the OEM gasket), the fit is better than some other pipes I've installed and still no CEL. I'm sure the CEL will come on sooner or later, knowing how OBDII works, but there is a cheap fix.
Go to radio shack and get a 1/4 watt, 1 meg-ohm resistor and a 1 micro-farad capacitor for all of about a buck and a half. Put the resistor inline with the 2nd O2 sensor's blue wire, and put the cap between the blue and white wire on the ECU side of the resistor.
Installing this pipe on a manual Protege5 wasn't bad either, and should have taken about 2-1/2 hours. All it took was the removal of the underbody plastic and the lower radiator hose. The clutch slave cylinder was still in the way, but a little force got past that.
The problem I did run into involved the EGR pipe nipple in the stock manifold. The nipple threaded out of the manifold instead of the flared tube nut coming off the nipple. No amount of penetrating oil would release it, and I removed the whole EGR tube from the car to get a better grip on it. My goal was to reuse the tube assembly, but the nut was so badly corroded to the nipple it was NFG.
I made a new assembly from 1/2" copper tube and everything was fine. From this effort I found that if you loosen the intake end of the EGR tube, its a whole lot easier to get it to line up with AWR header connection. The stock steel tube doesn't bend at all, and even a little mis-alignment would make connection nearly impossible without loosening the other end.
In the end it took me about 6 hours, 1 hour to locate a 26mm tube wrench (the intake manifold end of the tube is a b****), 2 hours to fab a new EGR tube and locate the right fittings and about 1/2 hour just to cuss my rotten luck. But none of this extra time can I blame on AWR.
Some low end performance was lost, which is the most noticable difference. But the car revs out much better now and I've changed how I drive and shift it. I shift about 1000 rpm higher now. Gas milage seems to have gotten much better, and I've now run several tanks thru just to be sure. Where I was getting an average of 30 mpg, I'm now getiing more like 35.
There is one minor nit with this pipe. The tail piece flange was touching the aluminum lower block on my test fit, so I ground it down. When I reinstalled it I had 3/8" clearance, but had failed to pull the mid pipe and grind it to match. So now the mid pipe forward flange is touching the lower engine block. Some day I'll have to fix that.