SharkDiver
Member
- :
- Speed3
So heres the story.I took my car to mazda for the motor mount recall and my car was fine.I got the car back 9 days later..Thats right 9 days...In the mean time my TXS race pipe came in.So I get my car back and I took it right home and installed the race pipe.When I took it out for a drive my boost would only go to about 15psi,It use to spike to 18 then hold 15psi.Now 4 days later my car will only go to about 13psi with no spiking to 15psi at all.I do not want to take it back to the dealer again unless I have too.I checked the vac. lines by the blow off valve and also put zip ties on the hose for the boost gauge but that is the only vac lines I looked at.I dont know what other ones to check out.
Could this for some reason be caused by the race pipe?What other vac lines should I check?
Any ideas on what I should do or check.This really sucks because my car has no balls any more and my dealer isnt the greatest at finding problems that are not coding.
Shark
Could this for some reason be caused by the race pipe?What other vac lines should I check?
Any ideas on what I should do or check.This really sucks because my car has no balls any more and my dealer isnt the greatest at finding problems that are not coding.
Shark
Last edited: