Ready to build my MazdaSpeed

I got the clutch installed had to remove and reinstall twice. There was what I thought was chatter form the Clutch disk but turned out to be a bent rod or something, I am not sure yet dropped the engine out the bottom of the car on Sunday and I will work on pulling it apart through out the week.
I am vary dishearted right now. I bought the back up block so that I would have time to do the upgrades I wanted on a better time frame. Pictures will fallow.
 
Engine block I picked up from LKQ
https://www.dropbox.com/s/iz0kub43gjv7tg0/IMAG0210.jpg?dl=0

https://www.dropbox.com/s/7bnh2sp5lo6v7ih/IMAG0211.jpg?dl=0

https://www.dropbox.com/s/vv5lnwppsy1mp1q/IMAG0216.jpg?dl=0

5th gear I picked from a 626 it's taller then my MazdaSpeed 5th from people have experienced it should be a drop of 800 to 1000 RPMS for 5th
https://www.dropbox.com/s/0it93z8gqfan5d3/IMAG0212.jpg?dl=0

Spare intake that I am removing all butterflies from and port and polish.
https://www.dropbox.com/s/boho2hp3dlpk3gx/IMAG0213.jpg?dl=0
https://www.dropbox.com/s/wsz0f4hcd31sij1/IMAG0214.jpg?dl=0

Here's a 626 mainifold which I decided not to use since I have an extra stocker
https://www.dropbox.com/s/noevkzzto28scme/IMAG0215.jpg?dl=0

Cam Gears off of the 626 one pick up on them could be useful for tuning maybe.
https://www.dropbox.com/s/a1k0xhqt25mjag6/IMAG0218.jpg?dl=0

Nice new clutch old one had 5000 miles left on it maybe. But the throwout bearing was bad.
https://www.dropbox.com/s/w8uffr5udb0cx03/IMAG0303.jpg?dl=0

Helper was tired
https://www.dropbox.com/s/921a80mix938oc8/IMAG0315.jpg?dl=0

So that's what was wrong all along I had a gremlin
https://www.dropbox.com/s/uzxs8q7dt0vxjfd/IMAG0318.jpg?dl=0
https://www.dropbox.com/s/0myuzc44o3681mj/IMAG0316.jpg?dl=0
https://www.dropbox.com/s/7f9l87beqpmxuq0/IMAG0319.jpg?dl=0

engine is pulled and needs to go on the stand
https://www.dropbox.com/s/fvme967j3oeuxxx/IMAG0320.jpg?dl=0
 
The oe compression ratio is not 9.5:1, it's 9.1:1.
 
Block, head, Diff and intake are going to the machine shop today :-) I have 2x off everything so I will take both blocks and heads. Pope will be sending out orders soon, as the test fit is already done.
Every day after work I work on cleaning parts and repainting.
I think I will jump in the engine bay and replace the wireloom on the harness as it is dry and cracking.
 
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Update:

Stopped by the shop after work this morning, cylinder wall took a bit of damage so it will need to be bored out to two over.
I also inquired about head work and with the price I can't say no to having it done now rather then later. So a good valve job knife edge and port and polish. Half the price of getting one online that's already done

https://www.dropbox.com/s/hf3rsp4ubduazm3/IMAG0335.jpg?dl=0
 
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when do you think itll be up aand running again?

Hey Illa,

DocB has recieved my oil pump so I'm thinking engine reassembly middle of Jan and complition by the end of Jan.
By the way i think the rim painting has turned out great. I have 1 rim to do still so I will put pic's up with the wheels on the car as soon as the paint has cured on the last rim.
 
Yesterday the Oil pump, Pistons and bearings came back from DocB Thank you.
Today the short block was assembled oil squirters were a pita but we all know that.
With the last shipments coming in before the weekend I plan for the engine to go in the car first weekend of February.
 
To anyone that is still following this thread I’m sorry there hasn't been an update. I have been really busy with working on the car.

The assembly and install went off without issue but we all know that when you install a shiny new part it will reveal at least two broken parts.
So after the install we spent a good couple of hours tracking down all the oil leaks in the AN fittings for the DocB setup. Stopped all the oil leaks and preceded to break in for 100 miles, mind you the clutch was broken in at the same time. Dumped the oil and strained for metal. Nothing to be alarmed about damn good machining job done at "Fast Moving Auto Parts" in Orlando, FL.
"Parts that failed in the first hundred miles, my hot pipe broke where it connects to the turbo, fixed with duct tape. The power steering pump went bad picked up low miles at JY.The MAF failed picked one up at the junk yard."
Filled her back up with fresh oil and new filter. Time to take the car on the interstate :-) Well first had to deal with an over boosting fuel cut issue. Ended up opening the waste gate all the way. Took all the tools and hit the on ramp. Holy crap she was fast this is off boost mind you. Sustained 120 mph for a few miles got off the interstate and that is when everything went downhill again. As soon as we got of the interstate the car shut off and the temp hit max! Long day short it was the ignition fuse. The O2 sensor wires had melted together. Auto parts store did not have the primary o2 so had to wait for a replacement.
I replaced the sensor and got back on the road. I had returned the CAN to a light pre load and was still having over boosting issues. "ThePope540"
Has been helping me deal with the issues.
Sense the CAN is working properly it seemed that it just was not working as fast as the turbo could build boost. Spikes of 15 to 21 psi. Pope suggested that I tap the turbo housing so the CAN would only see presser. My boost is stable at factory psi now but I still see fuel cut due to engine load.
I know I need an ECU option but I am holding out for the work Pope is doing on the stocker ECU. Not having an ECU option does not explain the great run I had at the interstate during the breaking.
I am stumped and add to everything else someone hit the car in my driveway while I was at work. I was devastated!
 
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