Hi everyone. I hope i can get some good feedback from anyone interested. I like how in this forum people are so willing to help others, so hopefully i can get this answered. I have a 2008.5 MS3 + Injen coldair, Turboxs DP and MP, Turboxs BPV, CPe rear mount, and hopefully if it will work a Turboxs MBC (I really want 18psi to finish the job because i dont want to do more mods than this).
This is a question to anyone that can help... I installed my Turboxs manual boost controller yesterday. the car ran great with the initial setting (boost controller turned all the way negative) it was doing like 8 to 10psi. I got to a nice empty open road by my house and started tuning. after a while of increasing the boost little by little, it suddenly went to like 24psi and the turbo screamed, then boost cut came and saved the day. now obviousle first you would think that "damn! a line blew off the actuator or compressor housing and im running open wastegate". not the case though, all lines where fine, so i uninstalled it thinking maybe the boost controller took a poop. ran it back to stock and it was fine. boost chillin at 15 to 16psi.now when i unistalled it i noticed that somehow i ripped the line that goes from the manifold to the top of the blow off valve. I replaced it before i tested it without the boost controller.
My question is, could this have caused it to run open wastegate???
This is a question to anyone that can help... I installed my Turboxs manual boost controller yesterday. the car ran great with the initial setting (boost controller turned all the way negative) it was doing like 8 to 10psi. I got to a nice empty open road by my house and started tuning. after a while of increasing the boost little by little, it suddenly went to like 24psi and the turbo screamed, then boost cut came and saved the day. now obviousle first you would think that "damn! a line blew off the actuator or compressor housing and im running open wastegate". not the case though, all lines where fine, so i uninstalled it thinking maybe the boost controller took a poop. ran it back to stock and it was fine. boost chillin at 15 to 16psi.now when i unistalled it i noticed that somehow i ripped the line that goes from the manifold to the top of the blow off valve. I replaced it before i tested it without the boost controller.
My question is, could this have caused it to run open wastegate???
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