I don't mind removing the turbo again, I just want it to make boost. (Full story of the car so we are on the same page: Purchased car with blown motor, 110k. Swapped JY motor and reinstalled turbo, car runs great no vac leaks and very smooth just will not push boost. Ebay fmic kit and relocated maf with no apparent leaks.) There was oil in the hot pipe and a small pool in the intake when I first pulled it because it would not build boost.
You can tell from the pics the turbine wheel is not damaged, the blades and the housing are perfect. I can try another wastegate actuator but it definitely has a good amount of tension on the wg flap, it takes some force to move it. What can cause a turbo to blow oil and not build boost? I assume it would be the seals inside the center cartridge behind the compressor wheel. Is there anything else it could be?
I would like to believe this turbo is ok, PO said the car pushed 8psi all day but I purchased it from another guy who only had it long enough to put 1k miles on it (and blow it up). Hard to believe the turbo and motor could both be bad. No shrapnel made it through the engine when the #1 rod snapped, the head and manifolds were fine so no particles could have damaged the turbine wheel as far as I know.
As mentioned earlier, we can refurbish them but not rebuild. Garrett does not release internal components for the bb turbos and we can only clean and rebalance reasonable working units. If any components are damaged we have to offer replacement cartridges (CHRA). I'm interested to see what your issue ends up being. I could see the turbine housing swing valve being stuck open and then fiddling with it allows it to close, then it sticks open again.Congrats on your new baby that is nice to hear, I found a GT2554r from an MSP with 45k miles I plan to replace the bad turbo with. I can remove the housings again and get a better look at it but the compressor side wheel does not have any damage and after messing with the WG flapper from the outside without removing the S pipe the car did start to push 6psi of boost and it did so 4-5 times before it went back to not boosting which really puzzles me and makes me think this turbo is ok. I still cannot figure out why it won't build boost, maybe it is the wastegate actuator. How much is it to rebuild a BB turbo at the shop you work at?
I removed the S pipe and hammered the sleeve for the WG flap back in and it moves easily with no binding or scraping of the housing when I had it off the car. Cannot figure out how it was able to push boost for a few minutes then back to no boost.
What brand clay bar, polish, and wax did you use?
Yeah I did, I got tired of waiting. Lol. Thanks!I used Meguiar's clay bar kit, Ultimate polish and Ultimate paste wax. Looks like you already did yours though. It looks great!