Mike, did you do a base line dyno?
Before the changes? Yes. IT's posted earlier in the thread.
If you mean when I first got hooked up to the dyno this time, then yes, though we weren't concerned with the results, it was just a run to make sure that the existing tune was safe and no knock.
12psi a year ago on that dyno with about the same conditions was 202whp 197wtq.
12psi this time we could only get to 170s wtq and 160whp. Boost just kept falling off to the 5-6psi range at redline. Turning up the boost was only spiking the peak torque a bit more each increase, but not really changing high RPM boost.
The HP line on the graphs was landing in the same point regardless of what boost we threw at it, which really suggests that something is capping the total airflow through the system.
I may have missed this, but Mike do you have cats?
Yes, I have 1 cat, it is a metallic core, 50,000 mile warranty, and sold specifically in the turbo exhausts by FM, so it is pretty much sure to hold up to turbo abuse. And this one was installed with the new turbo, so it only has about 4,000 miles on it.
I'd expect the boost taper on a DISI car, as a lot of those guys do that, but not on a Miata. Weird.
Well, I have more.
I re-did a boost leak check without turning down the boost controller first (like I did before the dyno day). The turbosmart MBC was audibly leaking, and the more I turned up the boost knob, the louder and faster the leak was, to the point of visibly vibrating the MBC. I connected the air pressure source directly to the boost controller on the signal side, leaving the wastegate line attached, and even at 1psi of air being fed to it, is is leaking slowly from the bleed-off holes in the side. Leaks more the higher the pressure i feed it, as well as the higher the boost is turned up. It would explain why my boost fall off a year ago was pretty similar to the boost fall off this time around. Last time I figured it was just the stock turbo running out of breath and having trouble maintaining boost. I had the same MBC controller then though, and never detected the leak.
However...
Removing the MBC and connecting the signal line directly to the wastegate with nothing in between, I still can't hold boost. I can't even get to the 6psi wastegate, stops rising around 5psi and then falls off to 2-3 psi, which doesn't fit a "cap" to power as much, since that is definitely below the peak power we were getting.
The primary suspect at this point is that the SS studs that came with the kit originally (because the iconel studs were on backorder) have stretched, and the turbine housing is just venting the pressure. I don't hear it at all, if anything the sound becomes more muted, not louder, so I would still think that fits a clog of some sort better.
Well, I am pulling the exhaust later on today, from the end of the downpipe all the way to the tips. Going to inspect it all, and take it for a drive uncorked, and log the boost again. I should have a power gain anyway, but if I can suddenly hold boost, then my exhaust piping is causing my problem.
If I still can't hold boost, then the next step will be to pull the turbo saturday morning, and since the water is going to be drained, I'm going to pull the radiator and sway bar while I'm at it, to check the timing belt's timing for the crank and cams, just in case (but I highly doubt that they are a problem).
And while the turbo is out, I'm going to pull the intake piping to inspect all of that for any clogging/restriction.