Removed the AWR and welded it up. It was split perfectly down the seam. Only reason it didn't leak as bad as it should have was because of the ceramic coating. Had that not been on there, it'd have poured oil out. The turbo inlet gasket had a small leak, and fortunately, getting to the transmission side oil pan bolts requires the removal of the downpipe, so I was already half way there. Also rerouted some of the harness and secured a few things to make the engine bay more "clean". After that I battled with the couplers/charge pipe blowing off on the hot side all night Saturday and all day Sunday. Finally got it taken care of by flaring the end of the pipe with vice grips. I had lowered my boost down to 14psi and it held last night and this morning no problems, so it should be fixed. Pep Boys carries Vibrant parts if anyone ever needs something in a hurry and you've got one locally. I've got an okay tune on the car now, too. Keeping the AFR's around 11.3-11.5, but I'd really like to nail them down to the 12-12.5 range to get some good power. Still haven't changed the timing tables, though.