about 8 days after I ordered the new radiator, it arrived in the mail. I was looking at the label stamped on it and it says denso (same as oem). However, on the one I blew up said "denso japan" but the new one says "denso china". Maybe not a big deal, but ideally, Id rather have something made in japan rather than china. Either way, I swapped the new rad in with no issues. Once I had it all together and filled with water, I began my journey home. About 10 mins later I'm on the interstate and I look up at my temp gauge. It was overheating again. I immediately got off on the next exit and found a good place to pull over. It had overheated, but it didn't quite reach the top of the gauge this time. I sat for about 30 mins and got back on the road. I would be able to get about 5 - 10 mins driving in before I needed to pull over and let it cool for about 30 mins. Needless to say, it took a while to get home. Thinking about it, I had replaced the broken radiator, but I didn't replace the thermostat. I wasn't completely sure that's what it was, but I was about 85% positive. Along the way I stopped into an auto zone and picked up a thermostat and a gasket for about $10. The gasket didn't look right to me, but the guy ensured me it was the right one.
I pulled up to the restaurant about 4 hours after my departure. My car needed to cool down, so I installed my vacuum block while waiting. Before the block install, my boost gauge, bov, and wga were all connected to the same hose. By the time I was done, my car was cooled down enough to get started. I drained the fluid, and took the thermostat housing off. Like I suspected, the gasket I was given was wrong. Luckily enough the rubber ring gasket that was already on there was still in good enough shape to reuse. I bolted it all together and filled with new coolant. After she was all buttoned up, I went for a spin. The thermostat was definitely the problem. I drove around for a while and the gauge stayed right where it should.
Also with the new block, it was evident that I had too much pulling off the one hose. I connected my bov(4mm) and wga (5mm) to the block and my boost gauge directly to the intake mani. I had also purchased a Boomba racing check valve to put before the wga. I know that wga's don't like vacuum, but the stock setup had no check valve. So to try to extend the life of my wga as much as I could, I figured taking vacuum out of the equation couldn't hurt. The block made a huge difference. Before the block, I had the turkey pretty bad even when shifting at ~2500 rpm. Now the turkey was almost completely gone. In fact, I really saw how much better my bov worked compared to before. Now instead of a lil hiss and a gobble gobble, the bov made a more profound swooshing sound when venting boost. The wga worked great as well. My boost was about 7.5ish psi with no spikes. I see now that getting the turbosmart wga was, in fact, smart. And on top of that, the turbosmart is easily rebuildable if the diaphragm were to rupture.
So now that my baby was up and running again, it was time to get back to my original goal: to fix the damn idle. My guess is I still have a vacuum leak somewhere. I plan to redo all the vacuum lines soon, so hopefully ill tackle the problem in the process.