Nice to see the update! Where are you getting the ZE from?
Tyler/Suprakid366's partout on PT. I got a message from Monoxide that his motor wasn't running right and he was losing to DE's, though, so I'm kind of second guessing things now. I think that was more in the past, and Tyler said he got the K6F manual tensioner as the belt had slack and had skipped a tooth, along with leaky injectors causing it to bog under load.
He still isn't pulling primo compression numbers, and this is copied from his thread:
"Back in winter when we first got the motor in the car and had big issues with the fuel injectors and rails dumping fuel into the motor, the engine compression tested with 208-210 on every hole. 2 weeks ago compression tested it in summer with a new battery, engine warmed up and the numbers are:
195 189 190
190 197 194
This test was very weird. Each first puff the needle would go past 60 psi which is good. But once it hit around 180 about the needle would move slightly on each compression stroke. But it would keep going. But once we got these numbers the motor was on i would say the 10 puff so we just stopped."
Source: forums.probetalk.com/showthread.php?t=1701302335
I'm kind of thinking the motor might have a decent bit of mileage on it, as the p/s pump has been replaced, the tensioner failed, and the injectors started leaking, on top of the sub-optimal compression numbers. I need to call him again and talk things over. For what he was asking, I thought everything was in tip top shape. He told me the motor had about 1500 miles on it, but that was since the head rebuild, so who knows what's on the bottom end.