ok, so there were some problems. first the temp was in the 90's and the two little fans they had didn't do much, cuz of the high temps i was running crazy rich. luckily while they were figuring out the problems with the dyno and my ignition, i was able to tune it a little better. apparently the WOT BOX was ******* wit the ignition. the first two runs the middle of the graph was cut out. i told them it was a wastespark ignition, and he set it for that but apparently the guy said it kept cutting in and out of wastespark, wtf??. luckily the the WOT BOX wires were easily accessable and i was able to grab the wire leading to the WOT BOX and that worked perfect on the 3rd run. i gotta email N2MB about this
also as you can see on the graph they read 13.7psi, afterwards i checked my boost controller and the FTC datalog and i barely broke 12 psi. around 11.8-12.3psi. had i know that, i woulda cranked up the boost a little more. lol
but i said 260 and i got there. lol
for AFR, the dashed line represents 11.8AFR